Gainesville Visit
So I came back from Gainesville yesterday, without having run down the quarter. But before we get to that, a couple of things went down. On the way to Gainesville, I noticed that wide open throttle was causing a misfire. I thought it was the recently installed boost controller, which, I do think was part of it. So, I called an old friend who was kind enough to let me use his garage and tools. Grant and I bought a new set of plugs and installed them. Turns out, NGK heat range works backwards. So while my “new” (currently removed) plugs were a numerically lower heat range, they were instead warmer. Anyway, we pulled those and installed a new set of copper ngk plugs, “6″ heat range. I also revised the mounting of the boost solenoid. Problems all solved, I think the plugs were the main issue. Anyway, next, we put Grant’s awesome RaceLogic performance box to work and recorded a few 1/4 mile passes. Back and forth over very flat ground. Either direction yielded very similar numbers with horrible launches. Trap speeds were all 109-110. ET was 13.2-13.4, 60ft was 2.1-2.4.
This box is very nearly exactly accurate to Gainesville raceway’s times (always within a tenth, I believe). So, I’m pretty happy with those times, especially considering that a hulking Grant was always in the passenger seat. I think better times, still are possible, even at nothing beyond 7.5 psi spikes.
The following day Kpeng and I went to the Bahamas for a drive.
video HERE RUN FIREFOX AND INSTALL DIVX PLUGINS







